Friday, 6 January 2012

Valve Clearance Set

Valve clearance adjusted. Intake side was OK. Exhaust side was too tight. Opened up to 0.007".

Flywheel Key Not Broken

I did find a chunk of the aluminum boss that broke off from the idler gear. Still worth pulling the flywheel.

Homemade Puller. Thanks Eric.

Key wasn't sheared off like I suspected. Now I'm stumped as to why the timing is slightly off. Oh well, we'll see if it runs and then worry about it.

Thursday, 5 January 2012

 New stainless studs for the exhaust, cut from M6 SS threaded rod. New exhaust gasket too.




New gaskets and wire brushed the carbon out.

Timing Off Slightly


With the "T" lined up in the hole on the cover, the line on the cam chain sprocket won't line up with the upper mark. It's either on one side or the other. Somehow the timing is off just a bit. As far as I can tell, the flywheel must not be in the correct position, which means that the key must be broken. I guess I will pull the flywheel and confirm.